Follow these vibration-reduction tips to achieve some rewarding audio results.
A manila folder dwelt for a long time in my file cabinet with a hastily scribbled,
unimaginative title on the tab — ”Preamp X.” I had started a pre amp project
nearly 20 years ago and collected data for that end, but ultimately let the
whole affair lie dormant, as I realized that my design ideas weren’t “high
end.”
Not so long ago a friend sent me some suggested circuits and parts recommendations
which looked very inviting, so after I scrapped old boards and unused documentation
and resurrected a half-made chassis, Preamp X was finally born (Photos 1 and
2).
PHOTO 1: Preamp X (with medical stethoscope to detect troublesome noises).
PHOTO 2: Preamp X insides.
This article is not a preamp construction project at all, but rather documents
what happened to Preamp X once it began to reproduce sound. I offer excerpts
from my log of Preamp X to illustrate the difficulty in properly finishing
even a simple piece of electronics in a way that brings out the best of its
realistic musical potential.
BASIC FEATURES
Preamp X houses two PC boards mounted on edge. One board contains two op
amp phono stages (with inductor RIAA rolloff), while the other contains a
pair of op amp line drivers. Separate regulators provide power at each opamp
supply pin. The raw supply is located behind a bulkhead to success fully reduce
the radiation of noise into the circuitry.
There is a five-way input selector switch, a blue Alps volume control, and
similar balance control. Toggle switches provide “muting” and “mono” functions.
The preamp was built into a Sunix chassis made of 0.035” steel (six elemental
panels) with an aluminum front dress panel. As you can see, in no. way is
Preamp X electronically or mechanically unusual, although component selections
followed the designer’s exhaustive testing.
FIRST VOYAGE
After the customary startup debugging and tweaking, the preamp came alive
and began turning out “promising” sound, meaning I didn’t think the promise
was fulfilled. Certain aspects of the music were acceptable, but the mainly
bland presentation was far from “live.” So I began a carefully documented
witch hunt to determine whether vibration was a factor. (The preamp has always
rested on four Sorbothane feet, a practice I ob serve for all electronic components.)
THE LOG
I have separated out the mechanical change items from the current total of
32 entries in the project logbook for the preamp, and repeat them here along
with their noted sonic consequences.
Where I underlined my logged comments, upper case is used here. Similar
entries accompany the electrical alterations, but those are not the subject
of this article.
In many cases I made several physical changes at once, clouding the issue
of which produced the most sonic improvement. If I build another pre amp,
I would complete all items listed during the initial construction phase, because
they all tested successfully. The basic mechanisms I attacked were panel and
component resonance and colliding objects:
2. Coat opamps and raw supply caps with lead foil (two layers). Note gains
in detail, bass, linearity and clarity.
3. Coat all mating cabinet surfaces with lead foil. Put long strips on top,
bottom, side panels. Improvements similar to 2 above.
9. Mount PC board L-brackets to grommeted holes instead of bare chassis metal.
Small improvement in clarity.
12. Mount front-to-back ¼” x ½” oak. strips on top, bottom covers (two each)
with Gorilla Glue (urethane based).
Add lead foil to power supply bulkhead. Apply remaining scraps of self-adhesive
damping “tar paper.” LARGE gains in detail, clarity, overtones, musicality.
15. While open (to replace phono coax cable), add more lead strips, some
foam, and rubber pads to combat vibration between the front dress panel and
the steel structural panel immediately behind it. Add foam dampers to the
long wires running between the input jack and selector switch. MAJOR IMPROVEMENT
in sound quality—sense of liveness, purity, dynamics.
It was startling to realize that items 12 and 15 were very successful AFTER
adding rubber grommets to the PC board mounts. However, the entire raw supply,
controls, and jacks are still hard- mounted except for the foam pad sup plied
with the toroidal transformer, so evidently something there is vulnerable.
Because the results are in hand, I won’t spend time isolating the culprit(s),
but some mystery lingers here.
DOWNSTREAM
The task of Preamp X is to drive a second electromechanical contraption,
“Amptron,” another collaboration using the designer’s electronic specifications
and my chassis.
Here I figured I had applied my structural lessons from Preamp X, but found
that Amptron still needed to undergo the same witch hunt, and that it too
reacted strongly to even more sophisticated vibration control than appears
here (the subject of another article).
FINDINGS
The inescapable evidence from these fruitful experiments is that electrons
should be the only moving parts in an electronic system. This can be trouble-
some to achieve depending on how loud the music plays, as I learned while
surveying the structures with a medical stethoscope, a very revealing instrument.
The sum total of these modest efforts resulted in a remarkable unveiling
of the musical presentation. Actually, I’d rather be telling you that the
changes are small and this effort was needless, but the fact is, Preamp X
has truly blossomed forth.
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